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Too long of a TrajectorySequence crashing opmode #361

@TheOutcastVirus

Description

@TheOutcastVirus

RR FTC Version

0.5.5

Observed Behavior

I'm currently initializing my TrajectorySequences in initialization in my LinearOpmode. Whenever a TrajectorySequence gets too long, however, the robot crashes in initialization and reports "stuck in stop()". I've tested this with all other interfering code removed, and the issue persists. If I run a identical opmode, but with 95% of the TrajectorySequence commented out (such that it is only one spline long) the opmode runs as normal.

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Robot Logs

robotControllerLog.txt

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